i think i found the problem with my motor
i think i found the problem with my motor
Last edited by Wolfpack Speed; 01-12-2007 at 12:59 AM.
Wolfpack Speed, Inc.4290 Campbells Run RdPittsburgh, PA 15205(412) 279-4902
JB weld it! lol!
Mike
Wolfpack Speed, Inc.4290 Campbells Run RdPittsburgh, PA 15205(412) 279-4902
nah duct tape!!!
01 GT Saleen Body kit & Wheels. BBK lowering kit and rear control arms, BBK 70mm throttle body, Trickflow upper elbow, BBK CAI w/K&N , and SLP cat back
Damn Mike! How tight did you have that belt???
-Paul
1995 GT 'vert
Best times on old 302 combo:
12.03 at 112.5mph NA
Best time with 9:1 compression NA dart block 331 setup:
11.50 at 121mph
Dyno'd: 415rwhp/410rwtq
2004 Z16 commemorative edition Z06
100% stock: 11.9 at 118mph
That sucks Mike. Time to build bigger and better!
1990 Mustang LX
naturally aspirated TEA Trick Flow R headed small block, C4, 3016 lbs, stock suspension, 28x10.5
9.36 at 143 mph
That sucks, time to get that alum block you been wanting.
"No man is entitled to the blessings of freedom unless he be vigilant in it's preservation"
General Douglas McArthur
it's whats for dinner
1969 Camaro restomod/project
1967 camaro
2011 mustang procharged
93 reef blue notch blk/int
92 calypso notch blk/int
86 t-type
1972 chevelle project
Not only did I fail at building a fast mustang but I bought a yellow zo6 cause I couldn't get my little dick up.
That sucks Mike. What do you attribute the failure to?
Mark
LeMans Blue Z06
hard to say guys. i do run a manual tensioner but i know for a fact i don't run it as tight as some people do. im know it adds extra stress on the crank but it really shouldn't have failed, especially from the tensioner. i have heard of a few faulty cranks from the factory and i wouldn't be surprised if mine was just weak or defective. it's really no big deal, im just happy i was able to et as well as i did on the oem long block...on to bigger and better things now
Wolfpack Speed, Inc.4290 Campbells Run RdPittsburgh, PA 15205(412) 279-4902
Thinking about it, that is probably Ford used a supported lower pulley setup from the factory. So the stress of the blower drive isn't way out there away from the front bearing and putting additional stress on the crank.
I did see somewhere that there was a reported failure or two on these cranks. Maybe you can take it in for warranty work? :)
Mark
LeMans Blue Z06
Wow, oh well time to do it the way you want now.
Sorry to hear.....guess a manual tensioner combined with a larger lower puts enough stress on the crank snout to snap it!! Yikes....
9.75 though.....sweet....
I heart alum. blocks.
-JOHN
Carburetors and SAE wrenches.................
Buy Made in the USA - It Matters.
That sucks...Build it bigger & better...
well i just think that crap happens
well i talked with Al Papitto last night. he pretty much confirmed what my self and many others figured to be the main contributor to the crank failure. i run a different aftermarket lower pulley setup which deletes the oem cage that adds extra support to the snout of the crank. i also run an aftermarket belt tensioner so that certainly adds more stress to the snout as well. Al said he has seen this happen before, this wont be an issue with the new combo!!!
Wolfpack Speed, Inc.4290 Campbells Run RdPittsburgh, PA 15205(412) 279-4902
Mark
Time for a new motor. Your crank might break. LOL
2016 Mustang GT
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